Article ID | Journal | Published Year | Pages | File Type |
---|---|---|---|---|
1756297 | Journal of Petroleum Science and Engineering | 2007 | 7 Pages |
In this study, Huff 'n Puff technique is used as a production mechanism to revaporize liquid dropout in the Saih Rawl retrograde condensate gas field, Oman. During the huff cycle, a number of wells were shut in to achieve revaporization. The same wells were put on stream, during the puff cycle.Liquid dropout induced a mechanical skin around the wellbore and hampered gas production capabilities but has been revaporized through pressurization. The pressure buildup in the rich-gas condensate reservoir was due to a cross flow originating from a deeper highly pressurized lean-gas bearing formation. The pressure communication was taken place through the wellbore during shut-in cycles.A compositional simulation model was used to confirm the theory of condensate revaporization. Simulation results indicated that Huff 'n Puff is a viable production technique. The technique improved gas deliverability and enhanced gas–liquid production by minimizing the skin caused by gas–liquid dropout.