Article ID Journal Published Year Pages File Type
5484636 Egyptian Journal of Petroleum 2017 14 Pages PDF
Abstract
Isomerization process became one of the best gasoline production sources, as it gives a high octane product while saving environment from pollution impacts. This paper presents a practical study that aims to improve the gasoline quality and economic income of an existing light naphtha isomerization unit used for octane improvement. The study included selecting the optimum combination of isomerization unit equipment that gives better product specifications for a specified feed. Eight scenarios were studied and simulated to predict the product specs. The original studied unit is MIDOR light naphtha isomerization unit at Alexandria-Egypt that recycles the unconverted hexane (C6). The other studied scenarios were adding fractionators for separating feed iso-pentanes, and recycling unconverted pentanes, hexanes and/or combinations of these fractionators. The results show a change in octane number of gasoline product for a specific feed. Once through process with no extra fractionators has lower octane number of 81 while that with de-iso-pentanizer-de-pentanizer and de-hexanizer produces gasoline with 92.3 octane number. Detailed economic study was done to calculate the return on investment “ROI” for each process option based on equipment, utilities, feed and product prices. Once through simple isomerization unit had the lowest ROI of 14.3% per year while the combination of De-iso-pentanizer with the De-hexanizer had the best ROI of 26.6% per year.
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Physical Sciences and Engineering Energy Energy (General)
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