Article ID Journal Published Year Pages File Type
55066 Catalysis Today 2012 8 Pages PDF
Abstract

In this work, the performances of WGS reaction carried out in a porous stainless steel (PSS) supported Pd-based membrane reactor (MR) have been experimentally investigated in terms of conversion, hydrogen recovery and hydrogen purity of permeate stream. A 20 μm thick Pd-based membrane prepared by electroless plating and a high temperature Fe–Cr based WGS catalyst have been used during the experimental campaign. Influence of parameters such as reaction pressure (from 7 to 11 bar) and gas hourly space velocity, GHSV (from 3450 to 14,000 h−1), at different steam to carbon ratio (from 1/1 to 4/1) has been investigated at the reaction temperature of 390 °C. As a best result of this work, by supplying a hydrogen rich-gas mixture such as 8% CO, 32% H2O, 24% CO2, 36% H2 to the MR operated at GHSV = 3450 h−1 and reaction pressure of 11 bar, almost 80% CO conversion, 70% hydrogen recovery with hydrogen permeate purity around 97% have been reached. Membrane fouling due to coke coverage on the membrane surface has been proven to be fully reversible: after 700 h of tests in WGS mixtures, H2 permeation and both H2/He and H2/N2 ideal selectivities remained unchanged.

Graphical abstractFigure optionsDownload full-size imageDownload high-quality image (101 K)Download as PowerPoint slideHighlights► Water gas shift reaction was performed in a Pd/PSS MR for high purity H2 production. ► At p = 11.0 bar, T = 390 °C, 80% of CO conversion and 70% H2 recovery were reached. ► The maximum H2 permeate purity was 97%.

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Physical Sciences and Engineering Chemical Engineering Catalysis
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