Article ID Journal Published Year Pages File Type
8072211 Energy 2018 17 Pages PDF
Abstract
In this paper a new method for the primary power control in TPPs is presented, based on the feedwater flow rate changes between the feedwater heaters (FWHs) and an additional high pressure economizer. The achieved primary power control reserve is demonstrated by measurements at the lignite-fired 650 MWe TPP after its retrofit by the installation of the high pressure economizer in parallel with FWHs. In addition, the TPP transient operation during the primary control are simulated and analyzed with the developed thermal-hydraulic model of the steam turbine heat regeneration system. The control reserve of approximately 10 MWe is shown both by measured data and results of numerical simulations. The control reserve is originally provided by the fresh steam throttling in front of the turbine, but this throttling can be reduced by the application of the new method. The rates of change of wall temperatures of FWHs tubes are within allowed limits during the transients.
Keywords
Related Topics
Physical Sciences and Engineering Energy Energy (General)
Authors
, , , , , ,