Article ID | Journal | Published Year | Pages | File Type |
---|---|---|---|---|
8077558 | Energy | 2014 | 8 Pages |
Abstract
A modeling study was performed to investigate the direct impact of amine CO2 scrubbing on the efficiency of a coal-fired power plant. The full scope of the capture process was simulated with 8 m PZ (piperazine) to estimate the steam, electricity, and cooling water requirements. The steam cycle was simulated for applications of the capture technology to both retrofit and greenfield (optimized new build) coal-fired power plants. The reboiler duty of the stripping column had an optimal molar L/G (liquid to gas ratio) of 4.9 in the absorber and the maximum reboiler temperature of 150 °C. Integration of this CO2 capture with a greenfield coal plant yielded an identical optimal L/G, but the optimal reboiler temperature was 140 °C, and the decrease in power plant efficiency was 7.3%. The retrofit case resulted in an optimum case with an L/G of 5.9, a reboiler temperature of 120 °C, and a decrease in plant efficiency of 7.0%. When running at the optimal L/G, the optimization sensitivity to the reboiler temperature was low.
Related Topics
Physical Sciences and Engineering
Energy
Energy (General)
Authors
David H. Van Wagener, Ulrich Liebenthal, Jorge M. Plaza, Alfons Kather, Gary T. Rochelle,