Article ID Journal Published Year Pages File Type
4987492 Chemical Engineering Research and Design 2016 14 Pages PDF
Abstract

•A pressurised spouted bed reactor is commissioned for study of gas-solid kinetics.•Accurate kinetic measurements can be made using the reactor.•A comprehensive method for extracting intrinsic kinetics is proposed.•Consistent intrinsic kinetics are obtained for reduction of Fe2O3 with CO.•The work provides a solid basis for further modelling of reaction dynamics.

A high pressure and high temperature spouted bed reactor, operating in fluidisation mode, has been designed and validated at low pressure for the study of gas-solid reaction kinetics. Measurements suggested the bed exhibited a fast rate of gas interchange between the bubble and particulate phases. Pressurised injection of the particles to the bottom of the bed allowed the introduction of solid reactants in a simple and controlled manner. The suitability of the reactor for the purpose of kinetic studies was demonstrated by investigation of the intrinsic kinetics of the initial stage of the reduction of Fe2O3 with CO over multiple cycles for chemical looping.Changes of pore structure over the initial cycles were found to affect the observed kinetics of the reduction. The initial intrinsic rate constant of the reduction reaction (ki) was measured by using a kinetic model which incorporated an effectiveness factor. The uncertainty arising from the measurement of particle porosity in the model was compensated for by the tortuosity factor. The average activation energy obtained for cycles three to five was 61 ± 8 kJ/mol, which is comparable with previous studies using both fluidised beds and thermogravimetry.

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Related Topics
Physical Sciences and Engineering Chemical Engineering Filtration and Separation
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