Article ID Journal Published Year Pages File Type
620920 Chemical Engineering Research and Design 2012 6 Pages PDF
Abstract

In view of high energy consumption and poor flexibility in boil-off gas (BOG) recondensation operation at liquefied natural gas (LNG) terminals, a flexible and cost-effective optimization including the control system and flow process has been proposed. The optimized control system maintains BOG recondenser pressure via the condensing LNG flow and recondenser liquid level via bypass LNG flow. A BOG recondensation process with pre-cooling operation utilizes high-pressure pump LNG to pre-cool compressed BOG before it is directed into recondenser. The engineering application in a case of 6.69 tons/hour (t/h) BOG and LNG output fluctuating between 49 t/h and 562 t/h shows, after the flexible and cost-effective optimization, that process energy decreases 91.2 kW, more 1.28 t/h BOG is recovered when LNG output load reaches the valley, and the operation stability is well improved.

► Optimization of control system and flow process to BOG recondensation. ► Control of condensing LNG flow is based on pressure within recondenser. ► Control of recondenser bypass LNG flow is based on liquid level within recondenser. ► BOG is pre-cooled by cold send out LNG flow before directed into recondenser.

Related Topics
Physical Sciences and Engineering Chemical Engineering Filtration and Separation
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