کد مقاله | کد نشریه | سال انتشار | مقاله انگلیسی | نسخه تمام متن |
---|---|---|---|---|
1741210 | 1017380 | 2011 | 6 صفحه PDF | دانلود رایگان |

The physics principles for maximizing the fertile to fissile conversion were used in developing reactor concepts for large scale utilization of thorium in thermal and fast reactors (Jagannathan & Pal, 2006; Jagannathan et al., 2008). It is recognized that these principles are very well suited for ‘He’ gas cooled reactors with graphite moderator since both helium gas coolant and the graphite moderator have low neutron absorption characteristics and thus gives better neutron economy. In this paper, these ideas are applied to the High Temperature Test Reactor (HTTR) core of Japan to assess its advantage over the present day gas cooled reactors. HTTR is helium cooled and graphite moderated system. Significant amount of thorium has been loaded in the HTTR core with some minimal changes in the existing core design. The modified design is called HTTR-M core.In the HTTR-M core, the fuel is changed from enriched UO2 fuel to Pu in ThO2 fuel. The locations of boron type burnable poison rods within each fuel assembly of HTTR are replaced by one cycle irradiated thoria rods. Also, the B4C type control assembly around the HTTR core is replaced by fresh seedless thorium assembly. The fertile thoria assembly are scattered uniformly in the HTTR-M core. The equilibrium core of HTTR-M shows very small burnup reactivity swing. The core excess reactivity is ∼18 mk at BOC and reduces to 1 mk at 660 days. It is interesting to note that this small reactivity change is intrinsically achieved by the choice of seed and fertile dimensions and their contents without the use of burnable poison rods or mechanical control rods which are used in HTTR core. The burnup reactivity swing in the latter after using burnable poison is ∼100 mk. The fissile seed inventory ratio (FIR) in a fuel cycle is 0.90 as compared with 0.717 of HTTR core. Since 233U is a better fissile nuclide with highest ‘η’ value in thermal range, the above conversion ratio can be regarded as quite good.
► Physics Design Principles for maximizing fertile to fissile conversion was applied to HTTR core.
► Modified design is called as HTTR-M core.
► Discharge Burnup is 55,000 MWD/T.
► Core excess reactivity is 18 mk at BOC and reduces to 1 mk at 660 days.
► The FIR is 0.90 as compared as compared to 0.717 of HTTR core.
Journal: Progress in Nuclear Energy - Volume 53, Issue 7, September 2011, Pages 814–819