کد مقاله | کد نشریه | سال انتشار | مقاله انگلیسی | نسخه تمام متن |
---|---|---|---|---|
755080 | 895922 | 2014 | 8 صفحه PDF | دانلود رایگان |
• A failed interfering part corresponds to steam turbine journal bearing examined.
• Surface damages such as crushes, cracks and micro-grooves observed.
• Chemical composition and microstructure not changed after failure.
• Fretting fatigue determined as the main failure mechanism.
• With appropriate assembly and accurate clearance failure can be diminished.
Journal bearings as so sensitive parts of steam turbines are very susceptible to failure through different mechanisms of wear, fatigue and crush during service conditions. Failure occurring through these mechanisms lead to turbine completely shut down as a result of interfering in working conditions of bearing different parts. In this research, failed interfered part of a journal bearing related to a 320,000 kW steam turbine was examined. Failure analysis investigations were performed by utilizing of stereographic, optical microscopy, scanning electron microscopy (SEM), energy-dispersive X-ray spectroscopy (EDS) analysis and hardness test. Surface crush, large amounts of surface cracks, no noticeable changes of failed surface chemical composition and microstructure with significant hardness improvement were the main obtained results. The studies were revealed that the bearing part loosing and inappropriate clearance can produce relative displacements under cyclic gradient loading. This condition was detrimental for the service life of turbine journal bearing via failure through fretting fatigue mechanism.
Journal: Case Studies in Engineering Failure Analysis - Volume 2, Issue 2, October 2014, Pages 61–68