کد مقاله کد نشریه سال انتشار مقاله انگلیسی نسخه تمام متن
756921 1462459 2016 8 صفحه PDF دانلود رایگان
عنوان انگلیسی مقاله ISI
Root cause analysis (RCA) of fractured ASTM A53 carbon steel pipe at oil & gas company
کلمات کلیدی
موضوعات مرتبط
مهندسی و علوم پایه سایر رشته های مهندسی کنترل و سیستم های مهندسی
پیش نمایش صفحه اول مقاله
Root cause analysis (RCA) of fractured ASTM A53 carbon steel pipe at oil & gas company
چکیده انگلیسی


• Incident involving failures of 2-in. schedule 80 carbon steel (CS) pipe, connected to pressure safety valve (PSV) and carrying raw gas has caused serious supply disruption. Root cause analysis (RCA) was performed to identify the most probable cause of the pipe failure.
• In reference to the existing evidence deduced from the tests and substantial existing data the study revealed that the root cause of the pipe failures is attributed to the initial leak of the raw gas pipe.
• From the basic pipe material properties and behaviour, it is suspected that the failure was initiated by a crack, most probably longitudinal in nature.
• The crack or horizontal slit allowed high pressure gas to jet through, with the jet momentum getting stronger as the effective diameter of the slit increased.
• Over time the crack enlarges and breaks off into large chunk, resulting in the gaping hole as evident in the photo record.
• In view of crack initiation and propagation, it is concluded that the root cause for the failure of the pipe section is due to excessive thinning as a result of thickness reduction by intentional grinding.
• Further damage to the surface of already excessively reduced thickness occurred due to nominal pipe vibration during service.

Incident involving failures of ASTM A53 carbon steel (CS) pipe, connected to pressure safety valve (PSV) and carrying raw gas has caused serious supply disruption. This study was performed to identify the most probable cause of the pipe failure. It was conducted by reviewing the existing design, construction data and pipe material analysis using non-destructive techniques such as VT, PT, MT and UT along with metallographic, hardness and microscopic analysis. The investigation revealed that excessive material loss has occurred in both failure and its adjacent regions due to abrasive grinding, resulting in the formation of a through thickness flaw. These grindings were performed to accommodate the pre-installed piping spool to avoid alteration in the pipe position. RCA demonstrated that this rapid thinning of the steel pipe body later led to its failure. Metallurgical study using photomicrograph shows that the morphology of the steel material was consistent and did not show any evidence of internal corrosion or micro fractures. Further damage to the surface of already excessively reduced thickness occurred due to nominal pipe vibration and atmospheric effect during service. The research work described in the paper has a significant meaning to recognize the root cause of such failures in CS pipes and through given recommendations to eliminate future such happenings.

ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: Case Studies in Engineering Failure Analysis - Volume 7, October 2016, Pages 1–8
نویسندگان
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