کد مقاله کد نشریه سال انتشار مقاله انگلیسی نسخه تمام متن
297338 511755 2012 9 صفحه PDF دانلود رایگان
عنوان انگلیسی مقاله ISI
An aging assessment on ex-service Alloy 800 steam generator tubing
موضوعات مرتبط
مهندسی و علوم پایه مهندسی انرژی مهندسی انرژی و فناوری های برق
پیش نمایش صفحه اول مقاله
An aging assessment on ex-service Alloy 800 steam generator tubing
چکیده انگلیسی

To support SG life extension and plant life management, an aging assessment was performed on a number of ex-service Alloy 800 steam generator (SG) tubes removed from three CANDU®1 stations with service life spanning from 2 to 27 years. Laboratory tests and examinations were carried out to investigate the potential aging mechanisms of SG tubing. High-temperature electrochemical experiments were performed under simulated SG secondary side crevice chemistry conditions to determine the corrosion susceptibility of the ex-service tubing; metallurgical examinations were carried out to check the chemical compositions, grain size, and hardness of the ex-service tubing materials and secondary ion mass spectrometry (SIMS) analysis was performed to assess the potential surface chromium depletion and grain boundary segregation of the ex-service tubing. Based on the results from the assessment, no increase in the corrosion susceptibility or changes in metallurgical properties of the ex-service tubes resulting from aging were observed. SIMS top-down profiles did not detect any aging-related surface chromium depletion on any of the ex-service tubes. However, SIMS imaging performed on the polished cross-sections of the ex-service tubes observed boron precipitation at the grain boundaries. Since no archived tubing with the same heat number as that of the ex-service tubing is available for comparison, whether the boron precipitation at grain boundaries is attributed to aging through SG operation is not conclusive and needs further clarification. In addition, the impact of this boron precipitation on the integrity of Alloy 800 SG tubing needs further investigation.


► Aging assessments were done on ex-service Alloy 800 tubes removed from CANDU steam generators.
► After up to 27 years of service, no changes in corrosion resistance of the ex-service tubing were found.
► Metallurgical properties of all the ex-service tubing are still comply with the ASTM standards.
► SIMS profile observed no aging related surface chromium depletion on the ex-service tubing.
► SIMS analysis found no sign of sensitization in the ex-service tubing.

ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: Nuclear Engineering and Design - Volume 242, January 2012, Pages 91–99
نویسندگان
, , ,