کد مقاله کد نشریه سال انتشار مقاله انگلیسی نسخه تمام متن
657263 1458062 2015 10 صفحه PDF دانلود رایگان
عنوان انگلیسی مقاله ISI
Efficiency study of a gas turbine guide vane with a newly designed combined cooling structure
ترجمه فارسی عنوان
مطالعه کارایی یک توربین گاز با ساختار ترکیبی تازه طراحی شده
کلمات کلیدی
بازده توربین، طراحی ساختار خنک کننده، اثربخشی خنک کننده، تلفات خنک کننده خنک کننده بخار
موضوعات مرتبط
مهندسی و علوم پایه مهندسی شیمی جریان سیال و فرایندهای انتقال
چکیده انگلیسی

Efficient turbine blade cooling structure design with high cooling effectiveness and low cooling loss is essential for improving the efficiency of turbomachines. This paper designs a new cooling structure combining external film cooling and internal convection cooling for a 1/2 scaled down gas turbine vane. The superheated steam replaces the traditional compressor air as coolant for the internal convective cooling. Wind tunnel experiments are conducted on a linear turbine cascade at exit Mach numbers of 0.9, and exit Reynolds number of 1.2 × 106, in order to study the cooling effectiveness of this cooling structure. Then the cooling entropy creation due to inevitable cooling losses (including internal friction and heat transfer losses and external heat transfer and mixing losses) of air cooling and steam cooling is estimated and discussed. It is found that, the cooling effectiveness of the test vane with newly designed cooling structure is high (approximately 0.8) and uniformly distributed. The entropy creation of external air cooling due to external mixing is higher than the heat transfer, and for the steam convective cooling, the entropy creation due to internal friction is much higher than heat transfer in the cooling process.

ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: International Journal of Heat and Mass Transfer - Volume 80, January 2015, Pages 217–226
نویسندگان
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