کد مقاله | کد نشریه | سال انتشار | مقاله انگلیسی | نسخه تمام متن |
---|---|---|---|---|
8088824 | 1521906 | 2016 | 17 صفحه PDF | دانلود رایگان |
عنوان انگلیسی مقاله ISI
Hydraulic history and current state of the deep geothermal reservoir Groà Schönebeck
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کلمات کلیدی
موضوعات مرتبط
مهندسی و علوم پایه
علوم زمین و سیارات
ژئوشیمی و پترولوژی
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چکیده انگلیسی
The necessary infrastructure for production and subsequent injection of geothermal fluid was established in June 2011. Between June 8, 2011 and November 8, 2013, 139 individual hydraulic tests were performed with produced/injected volumes ranging from 4.4 to 2567 m3. The productivity index decreased non-linearly from 8.9 m3/(h MPa) on June 8, 2011 to 0.6 m3/(h MPa) on November 8, 2013. Five possible reasons for the productivity decrease are discussed: wellbore fill, wellbore skin, the sustainability of induced fractures, two phase flow and compartmentalisation. For all hydraulic tests, the injectivity index remains almost constant at 4.0 m3/(h MPa). During 17 of 139 hydraulic tests a sudden increase of the productivity was observed. Possible reasons for this effect are discussed: accumulation of free gas and/or fines and scales within the fracture as well as changing hydraulic properties due to changing mechanical load on the fracture.
ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: Geothermics - Volume 63, September 2016, Pages 27-43
Journal: Geothermics - Volume 63, September 2016, Pages 27-43
نویسندگان
Guido Blöcher, Thomas Reinsch, Jan Henninges, Harald Milsch, Simona Regenspurg, Juliane Kummerow, Henning Francke, Stefan Kranz, Ali Saadat, Günter Zimmermann, Ernst Huenges,