کد مقاله کد نشریه سال انتشار مقاله انگلیسی نسخه تمام متن
10274705 461666 2016 10 صفحه PDF دانلود رایگان
عنوان انگلیسی مقاله ISI
Lab-scale investigations on catalyst recovery of gasified residue collected from the potassium-catalyzed steam gasification process
ترجمه فارسی عنوان
تحقیقات آزمایشگاهی در مورد بازیابی کاتالیزور از باقی مانده گازسیون جمع آوری شده از فرایند گازسیلی شدن بخار پتاسیم
کلمات کلیدی
بهبود کاتالیست، گازسوز شدن بخار پتاسیم، پاک زغال سنگ، بازده بهره وری، رآکتور باربری تحت فشار،
موضوعات مرتبط
مهندسی و علوم پایه مهندسی شیمی مهندسی شیمی (عمومی)
چکیده انگلیسی
The catalyst recovery process was investigated utilizing different washing methods and operating conditions after potassium-catalyzed steam gasification. During potassium-catalyzed steam gasification, the H2 yield and carbon conversion (XC) could reach 101.18 g/kg-coal and 73.39%, respectively, when utilizing Lanna clean coal as a sample; the potassium compounds mainly existed in three forms: KAlSiO4, KHCO3, and K2SO4. In the catalyst recovery process, the highest recovery efficiency of potassium (ηK) on Lanna raw coal and clean coal gasified residue reached 92.14% after six limewater washings and 93.37% after three limewater washings, respectively. When utilizing the combined washing method for the Lanna clean coal gasified residue, the recovered catalyst showed a longer catalyst reuse lifetime even though the recovery efficiency of potassium (ηK) only reached 89.42%, which was 4% lower than that obtained after three limewater washings.
ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: Fuel Processing Technology - Volume 141, Part 1, January 2016, Pages 44-53
نویسندگان
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