کد مقاله | کد نشریه | سال انتشار | مقاله انگلیسی | نسخه تمام متن |
---|---|---|---|---|
1756297 | 1522895 | 2007 | 7 صفحه PDF | دانلود رایگان |

In this study, Huff 'n Puff technique is used as a production mechanism to revaporize liquid dropout in the Saih Rawl retrograde condensate gas field, Oman. During the huff cycle, a number of wells were shut in to achieve revaporization. The same wells were put on stream, during the puff cycle.Liquid dropout induced a mechanical skin around the wellbore and hampered gas production capabilities but has been revaporized through pressurization. The pressure buildup in the rich-gas condensate reservoir was due to a cross flow originating from a deeper highly pressurized lean-gas bearing formation. The pressure communication was taken place through the wellbore during shut-in cycles.A compositional simulation model was used to confirm the theory of condensate revaporization. Simulation results indicated that Huff 'n Puff is a viable production technique. The technique improved gas deliverability and enhanced gas–liquid production by minimizing the skin caused by gas–liquid dropout.
Journal: Journal of Petroleum Science and Engineering - Volume 55, Issues 1–2, January 2007, Pages 67–73