کد مقاله | کد نشریه | سال انتشار | مقاله انگلیسی | نسخه تمام متن |
---|---|---|---|---|
7168551 | 1462991 | 2013 | 10 صفحه PDF | دانلود رایگان |
عنوان انگلیسی مقاله ISI
Loss of a 30â³ directional crossing due to pipeline collapse during pullback
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موضوعات مرتبط
مهندسی و علوم پایه
سایر رشته های مهندسی
مهندسی صنعتی و تولید
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چکیده انگلیسی
This article concerns the loss of a Horizontal Directional Drilling crossing due to a failure that took place during pullback of the pipeline. The more than 500Â m long drilling was meant to lodge a 30â³ pipeline that crossed a large river. The failure caused the total loss of the crossing, and the necessity to repeat the entire process in another, less favorable location. Root causes involved a difficult soil composition, and constraints at a populated bank that led to engineering solutions not proved before on a pipe of such diameter. Discontinuities on the tunnel and the use of a sacrifice pipe at the front end of the pipe column, which was related to the need for more pipes than originally calculated because of a series of problems at the beginning of the perforation, were also defined as root causes. Lessons learned are highlighted.
ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: Engineering Failure Analysis - Volume 33, October 2013, Pages 388-397
Journal: Engineering Failure Analysis - Volume 33, October 2013, Pages 388-397
نویسندگان
Janine Booman, Hernan Kunert, José Luis Otegui,