کد مقاله کد نشریه سال انتشار مقاله انگلیسی نسخه تمام متن
774293 898162 2010 8 صفحه PDF دانلود رایگان
عنوان انگلیسی مقاله ISI
Failure analysis of an aero-engine combustor liner
موضوعات مرتبط
مهندسی و علوم پایه سایر رشته های مهندسی مهندسی صنعتی و تولید
پیش نمایش صفحه اول مقاله
Failure analysis of an aero-engine combustor liner
چکیده انگلیسی

The paper presents a failure case of an aero-engine combustor liner. Macroscopic and microscopic observations, microstructure investigation, chemical analysis and hardness measurement have been performed to investigate the damage mechanism and failure causes of notches and cracks. The results show that the failure modes of notches, axial-direction crack along the combustor liner and crack at the edge of welding spot are respectively attributed to high-temperature ablation, mixed crack of ablation and thermal fatigue crack. The bad configuration of crossover tube is the main reason for the failure of combustor liner.

ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: Engineering Failure Analysis - Volume 17, Issue 5, July 2010, Pages 1094–1101
نویسندگان
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