کد مقاله کد نشریه سال انتشار مقاله انگلیسی نسخه تمام متن
7104336 1460339 2018 18 صفحه PDF دانلود رایگان
عنوان انگلیسی مقاله ISI
Start-up improvement of a supplementary-fired large combined-cycle power plant
ترجمه فارسی عنوان
راه اندازی یک نیروگاه بزرگ ترکیبی با استفاده از نیروی تکمیل شده
موضوعات مرتبط
مهندسی و علوم پایه مهندسی شیمی تکنولوژی و شیمی فرآیندی
چکیده انگلیسی
The start-up time of a combined-cycle power plant depends mainly on the heat recovery steam generator (HRSG) with its thick-walled tubes. This work contributes to a start-up time reduction of a large combined-cycle power plant (CCPP) with a supplementary-fired HRSG. Hence, a dynamic simulation model is developed using the advanced process simulation software (APROS). The flue gas path and the water/steam side are modelled in detail. All control structures required for the plant operation are implemented, e.g. drum, steam turbine bypass system and steam temperature control. The comparison between model predictions and design data at different load changes shows high correlation towards given data with an average relative error of 5%. Using the developed model, hot, warm and cold start-ups are simulated and finally three different reduced start-up times of gas turbine (15 min, 24 min and 38 min) are evaluated. A comparison between baseline and improved start-ups reveals time saving and fast power generation rate.
ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: Journal of Process Control - Volume 64, April 2018, Pages 71-88
نویسندگان
,