کد مقاله کد نشریه سال انتشار مقاله انگلیسی نسخه تمام متن
774155 1462997 2013 9 صفحه PDF دانلود رایگان
عنوان انگلیسی مقاله ISI
Fatigue fracture of an AMX aircraft main wheel
موضوعات مرتبط
مهندسی و علوم پایه سایر رشته های مهندسی مهندسی صنعتی و تولید
پیش نمایش صفحه اول مقاله
Fatigue fracture of an AMX aircraft main wheel
چکیده انگلیسی

A forged 2014-T6 aluminium alloy main wheel of an AMX aircraft failed during pre-flight taxiing.Failure occurred on the wheel housing hub and its origin was located on the interior edge of the bearing cup housing. The wheel experienced high cycles fatigue. A plastic deformation was produced during the wheel mounting operations caused an abnormal stress concentration. It has been identified as cause of a progressive fracture mechanism. Consistent optical, metallographic and electron microscopy evidences were collected. Moreover, Finite Element Analysis (FEA) demonstrated that the observed defects produced the stress level needed to fatigue to initiate. Recommendations were issued in order to improve the Non-Destructive Techniques (NDT) used to monitor the wheel structural integrity. Laboratory tests showed that ultrasounds in this case would be far more efficient than the prescribed eddy currents.


► Failure analysis of a military aircraft fatigue case study is presented.
► Maintenance history and prescribed NDTs is considered.
► An alternative NDT inspection is proposed.

ناشر
Database: Elsevier - ScienceDirect (ساینس دایرکت)
Journal: Engineering Failure Analysis - Volume 27, January 2013, Pages 194–202
نویسندگان
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